GPS Glitches cause erratic behaviour and crashes in any GPS flight mode

Good Evening,

I have taken your advice and lowered the GPS antenna to just above the NAVIO2 on a aluminium foil platform. I have also reattached the Raspberry Pi using a number of foam sticky pads to attempt to reduce the vibration. Pictures attached. I then run it inside on the ground and here is the log file: https://plot.dron.ee/uXrt